1896 gt 2.8 with a 4t60 trans. It was running bad about a two months ago so I decided it was time to remove the intake and take a poke around. It also had a wire harness that had been spliced in many places so a new harness was also put on. It ran like a top! Then a month ago it started running like crap. It would buck and stall intermittently. So, it got parked until today. I got it up to temp and threw a scanner on it and got the following results. . Codes: 21,34,33 With engine readings. Block learn 124 TPS (v) 4.14 (isn't norm around .25 to 1.25? could it just be a TPS?) IAC POS 40 O2 crossout's 2/ changes A/F learned :NO Spark adv: 52 Basw PW: 1.5 MAT: 43C MAP KPA: 34 MAP (v) 1.38 .............................. I really doubt its a vac leak......
IP: Logged
10:22 PM
PFF
System Bot
Xanth Member
Posts: 6886 From: Massachusetts Registered: May 2006
I've also found a few situations where the TPS gets stuck in a position for one reason or other. If you haven't already, take a look and see if the TPS itself is just stuck in the wrong position. I mention that because the voltage reading you are getting is somewhere around full throttle.
IP: Logged
10:39 PM
87antuzzi Member
Posts: 11151 From: Surrounded by corn. Registered: Feb 2009
I was watching to scan gague while going from WOT to 0% during my "de bugging" drive and it would range from 3.25 to 4.XX. I also found another TPS that I just swapped on. The old one felt like it had rust in it. So its swapped over. Im going to go throw the scan gauge back on and go for another drive. YAY for reading vins at night to please the stupid scanner
IP: Logged
10:47 PM
87antuzzi Member
Posts: 11151 From: Surrounded by corn. Registered: Feb 2009
Its now 4.65 at WOT. So thats back in the norm. However its stalling at stops, has a hesitation from stop to WOT and misses where ever it pleases. However, im starting to wonder if its all electrical as the SES turns on and off when ever it pleases also...... So tomorrow I will check grounds, add a strap or two and check the C500 and C203 connectors for possible corrosion while im playing with the car. Stay tuned.
IP: Logged
11:13 PM
Jul 9th, 2011
85 SE VIN 9 Member
Posts: 690 From: Harwood Heights, IL, USA Registered: Apr 2010
Could the new harness have gotten loose or twisted or something? Did you look in the intake again? Maybe it's dirty again. Maybe there's a lot of blowby or something being recirculated through the crankcase ventilation system.
I hear tell the 1896 Fiero's had lots of problems...
IP: Logged
10:02 AM
Francis T Member
Posts: 6620 From: spotsylvania va. usa Registered: Oct 2003