Fiero 2m8 LT1 NX Roadster conversion (Page 19/46)
Jake_Dragon SEP 24, 09:38 AM

quote
Originally posted by Fiero2m8:


I do have Archie's front solid mount and the trans braced with a solid strut bar.
The top front of the motor still tries to twist rearward.
I'll post what I try next.



If your lucky you will only break bolts. The tranny is moving around and stressing your mounts thats why they are failing. Its also putting a lot of stress on your tranny and could cause it to fail as well.
Its a bad idea to mix the type of mounts you use, the car I pulled my V8 kit out of had mixed mounts and the front tranny mount was toast. Once it let go the rest of them started to fail.
Good luck
Fiero2m8 SEP 24, 04:01 PM

quote
Originally posted by tvelarde:


How did you modify the header to allow the clearance? I have gone through all my spare headers and many cast exhaust manifolds trying to gain sufficient clearance to get by my sppedometer housing, which looks identical to yours. Thanks for all the work you have done and for the boost to those of us not quite as intuitive as you are.



I took a standard SBC hugger header and cut the tubes at a 30 degree angle about an inch from the flange.
Then I had the muffler shop flip the flange over and reweld the tubes.
When you are done the angle that normally went towards the block now goes at the same angle away from the block (kind of like a mirror image).

Here's the progress today - my son Andrew convinced me to chop the top and paint the new roadster model for him - he also wants to swap motors with a Corvette model he has





Looks like I'd better get pros to paint my car
At least he says it "looks awesome"

Fiero2m8

[This message has been edited by Fiero2m8 (edited 09-24-2006).]

Fiero2m8 SEP 24, 05:02 PM
Update from yesterday's troubleshooting of a fuel pump that wouldn't shut off after ignition was turned off.

Did a search and found that most often it is a fuel pump relay or the oil pressure sending unit.

1) Unplugged the FPR - still kept running
2) Unplugged the oil sender - stopped
3) Going to replace both so I have a spare relay, since it wasn't easily available, and I can't swap it with the A/C relay in a future test like you can with a stock Fiero.

I believe I damaged the Oil pressure sensor when I accidently had it connected to a Tach signal wire from the ECM that has now been corrected.

Here is a shot of the GM part # for my relay and the ALDL connector right below it in the trunk:



Replacing the Oil pressure sensor ending up being a bigger job than I planned due to a lack of access!

Access to the Sensor was blocked by the IAC motor on the bottom of the throttle body.
Normally it wouldn't be a problem unless your intake is reversed like mine.
I tried removing the IAC but one of the two T-20 torx screws wouldn't clear the body of the Oil pressure sensor:



This meant removing the Throttle Body was necessary - it is held on by 4-10mm bolts.
The most time consuming part was cleaning the gasket surface using gasket remover etc. in order to prep for a new one.
Here is a view from the rear showing the hose connections, the top one provides crankcase vent to the rear valve cover. The middle one is a purge line for the vaccuum canister and the bottom one is capped, as I don't need coolant to warm the TB, as this car won't be winter driven. I took the time to clean the throttle plates with some brake cleaner while it is off:



With the TB removed, it is a direct swap of the sensors - the new one had sealant already on the threads.
Notice the arrangement of the two 90 degree fittings to keep it clear of the other sensors on the TB.



The hose in the centre goes to the PCV valve on the side of the intake manifold - if anyone needs info on anything else in these pics, let me know.



When I pick up a new TB to Intake gasket tomorrow, I should be back in business.

Fiero2m8


tvelarde SEP 24, 07:54 PM
WOW! Thanks for the fast response. I understand the concept and will go measure for the cuts. Thank you very much.

Andy
Fiero2m8 SEP 25, 01:29 PM
Look what the UPS guy delivered minutes ago:



Says "push" on both ends, so I guess it just plugs right in?

Anyone know where to open the ECM for the swap?

Here is a pic of my computer:

Fiero2m8 SEP 25, 03:26 PM
Well sometimes you just have to get off your butt and go out to the garage
Here are the steps as I discovered them:

1. Disconnect negative at battery (mine is in a sheet metal box in the front compartment)


2. Remove protective cover from ECM - (mine is homemade that fits in the trunk)


3. Remove 4 chip cover screws and gasket with 1/4" nut driver


4. Released two clips at ends of old chip and pull straight out


5. Chips can only go in one way due to keyed top centre and bottom left notches - in this case stickers were 180 degrees different between chips. Align notches and push chip in until you hear two clicks (the locking tabs moving back into place)


6. Re-install gasket/covers and battery negative.

Someone will search this one day and give me a + rating

Fiero2m8
Fiero2m8 SEP 25, 09:53 PM
Tonight I got all the harness wrapped using 1/4", 3/8",1/2", & 3/4" split loom.
Not the best stuff, but it was cheap and will do for now.
I had to make sure it stays well clear of the heat sources, so it doesn't melt:





On another note, I could smell gas, and it looks like I have a very small leak coming from under one of the support straps on the fuel tank.
I'm not really surprised given the number of times this original gas tank has been R/R over the last couple years.

I've also designed a solution to solve the melting knock sensor on the left bank, as it was too close to the header flange.
I should have those pictures by the weekend.

Always something, so I'll get at those items once I get the rear of the Fiero on car ramps again.
Bet you can tell I'm avoiding the dreaded bodywork

Fiero2m8
Fiero2m8 SEP 26, 10:25 PM
Well I went for a long test drive to get the ECM to learn some of its new programming.
Haven't changed the plugs yet which may be partly fouled, but the car is definitely idling better with the new chip.
I think I'm getting there with the tuning, but I still have to deal with high MAP (low vacuum) at idle and high IAC counts. The best news is the rich condition at idle is finally gone and the long term fuel trim stays near 128.

I plan to change the oil and plugs and then take some new readings with the scanner and try my new Datamaster Software with the laptop to log some data.

The bad news of the day is my Powermaster 9000 starter solenoid crapped out when I got home and I had to push it into the garage (first push since the rebuild)

This is the crap starter that I have killed two solenoids with:



Not sure how many teeth the Fiero auto flexplate has - that info would help for ordering purposes or does anyone know how many teeth the Powermaster 9000 is designed for?

On second thought, this was my second Powermaster 9000 in 2 years so I refuse to buy another!!!

What are my options?
I did a search and the PMR-9004 seems like an upgrade with better gearing, but I was worried it may be larger, not to mention it's still a Powermaster
Space is a premium with Archie auto setups. What do you SBC V8 guys using Archie's kit like the best?
I'm sure that relocating the new battery to the front compartment didn't help any either...
My LT1 is build with 10-10.5:1 compression and it complained while cranking with anything less than a full battery charge - matters got worse during hot starts!

------------------

1986 Fiero2m8 (LT1 NX / 4T60 Roadster Build)
http://www.fiero.nl/forum/Forum2/HTML/071642.html

tvelarde SEP 28, 09:49 AM
From the number of questions increasing on this site, there seems to be renewed interest in using the 4 speed automatic overdrive transmissions. You may have just started a great trend. If not, well then the rest of us that are in the midst of building one will continue to re-read every word as often as possible. I learn more everytime I read that thread.

Andy
Fiero2m8 SEP 28, 12:24 PM
Thanks Andy, plus for you (4T60 swap) - the funny thing is most of the questions are coming from me
PFF is great and I wish I knew about it before I registered earlier this year.

I looked back a few posts and realized I should provide some updates:
First to get the car on jack stands - I used 6 this time since the motor / trans are heavy and I didn't want to get squished




Since the fuel drip was so minor, it took a while to pinpoint the leak.
Eventually I cleaned this area up enough to create a pinhole so I knew what area to repair.
It was in one of the recessed areas, not under the strap as I previously had guessed.




This is the product I used for the repair as recommended by the muffler shop.
It is amazing stuff that dries quickly and allows you to build layers up on itself.
The best part is that since it is designed to fix holes in lawnmower gas tanks etc. it is not affected by gasoline!
Case in point - when I sanded and cleaned the area to be repaired, a tiny stream of fuel was peeing out and a small dab on my finger stopped the leak within a second. After 10 minutes I filled in the recess area with Seal - All temporarily held in with a piece of duct tape. I've seen this stuff used on seams too. I've also used cold weld in the past, but it only works when the tank is empty. Try it on a minor leak - it's like $5 and our tanks are getting old without an easy source for replacements...




My Knock Sensor project didn't go exactly as planned.
The 1994 iron head LT1 uses 2 sensors 1 almost touches the 4T60 tailshaft making plugging it in tricky and the other side burnt during my running rich problem after the rebuild.
My idea was to 90 it out of the way with pipe threads but I didn't have clearance to install this without removing the header
Since it didn't melt before the rich problem, I elected to replace it as before, but I wrapped the plug with some header tape as an extra precaution shown here:



The new sensor has sealant already on the threads, but make sure you're ready for a quick swap or you'll be wearing coolant at engine temp

I'm also a member on CamaroZ28.com and often research their LT1/LT4 tech and Nitrous pages for good info.
One of the problems I had lately with the idle was a very high IAC reading around 80 when 20-40 would be ideal.
With my new cam, it is looking for more intake air at idle, so I followed this procedure to correct it:

1. With the engine idling and the scanner on, I adjusted the throttle stop screw out (opening butterfly valves) until my IAC count was around 30 (my IAC learned # was 32)

2. Next I had to remove the TPS sensor as it was now at .9 volts and 5% open on the scanner. To correct it back to the middle of its 0.2 - 0.9 volt idle range, I drilled the holes into slots to allow rotational adjustment:


3. Then I reinstalled the sensor and set it at 0.58 volts with throttle position at 0% per scanner reading from ECM.

4. After everything was reconnected, I performed an IAC reset. For details check out this link thanks to "shoebox" -
http://shbox.com/1/4th_gen_tech2.html#iac_reset

5. Verified with scanner and immediately noticed less eratic idle and starts much better without throttle depressed

Fiero2m8

[This message has been edited by Fiero2m8 (edited 09-28-2006).]